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Apollo 13 Essay Research Paper Apollo 13

Apollo 13 Essay, Research Paper


Apollo 13 (AS-508)


Houston, we have a problem.


The Apollo 13 mission was launched at 2:13 p.m. EST, April 11, 1970 from launch


complex 39A at Kennedy Space Center. The space vehicle crew consisted of James A. Lovell, Jr.


commander, John L. Swigert, Jr., command module pilot and Fred W.


Haise, Jr. lunar module pilot.


The Apollo 13 Mission was planned as a lunar landing mission but


was aborted en route to the moon after about 56 hours of flight due to loss


of service module cryogenic oxygen and consequent loss of capability to


generate electrical power, to provide oxygen and to produce water.


Spacecraft systems performance was nominal until the fans in cryogenic oxygen tank 2 were


turned on at 55:53:18 ground elapsed time (GET). About 2 seconds after energizing the fan circuit,


a short was indicated in the current from fuel cell 3, which was supplying power to cryogenic


oxygen tank 2 fans. Within several additional seconds, two other shorted conditions occurred.


Electrical shorts in the fan circuit ignited the wire insulation, causing temperature and


pressure to increase within cryogenic oxygen tank 2. When pressure reached the cryogenic


oxygen tank 2 relief valve full-flow conditions of 1008 psi, the pressure began decreasing


for about 9 seconds, at which time the relief valve probably reseated, causing the pressure


to rise again momentarily. About a quarter of a second later, a vibration disturbance was


noted on the command module accelerometers.


The next series of events occurred within a fraction of a second between the


accelerometer disturbances and the data loss. A tank line burst, because of heat, in the


vacuum jacket pressurizing the annulus and, in turn, causing the blow-out plug on the


vacuum jacket

to rupture. Some mechanism in bay 4 combined with the oxygen buildup in


that bay to cause a rapid pressure rise which resulted in separation of the outer panel. The


panel struck one of the dishes of the high-gain antenna. The panel separation shock closed


the fuel cell 1 and 3 oxygen reactant shut-off valves and several propellant and helium


isolation valves in the reaction control system. Data were lost for about 1.8 seconds as the


high-gain antenna switched from narrow beam to wide beam, because of the antenna being hit and


damaged.


As a result of these occurrences, the CM was powered down and the LM was configured


to supply the necessary power and other consumables.


The CSM was powered down at approximately 58:40 GET. The surge tank and


repressurization package were isolated with approximately 860 psi residual pressure (approx. 6.5


lbs of oxygen total). The primary water glycol system was left with radiators bypassed.


All LM systems performed satisfactorily in providing the necessary power and


environmental control to the spacecraft. The requirement for lithium hydroxide to remove carbon


dioxide from the spacecraft atmosphere was met by a combination of the CM and LM cartridges


since the LM cartridges alone would not satisfy the total requirement. The crew, with direction


from Mission Control, built an adapter for the CM cartridges to accept LM hoses.


The service module was jettisoned at approximately 138 hours


GET, and the crew observed and photographed the bay-4 area where the


cryogenic tank anomaly had occurred. At this time, the crew remarked


that the outer skin covering for bay-4 had been severely damaged, with a


large portion missing. The LM was jettisoned about 1 hour before entry,


which was performed nominally using primary guidance and navigation system.

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